Overseas National Airways Flight 032

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Overseas National Airways Flight 032
Overseas National Airways McDonnell Douglas DC-10-30CF N1032F.jpg
N1032F, the aircraft involved in June 1974
Occurrence
DateNovember 12, 1975
SummaryBirdstrike resulting in an uncontained engine failure
SiteJohn F. Kennedy International Airport, New York, United States
40°38′N 73°46′W / 40.633°N 73.767°W / 40.633; -73.767Coordinates: 40°38′N 73°46′W / 40.633°N 73.767°W / 40.633; -73.767
Aircraft
Aircraft typeMcDonnell Douglas DC-10-30CF
Aircraft nameHolidayLiner Freedom
OperatorOverseas National Airways
RegistrationN1032F
Flight originJohn F. Kennedy International Airport, New York, United States
StopoverFrankfurt International Airport, Frankfurt, Germany
DestinationKing Abdulaziz International Airport, Jeddah, Saudi Arabia
Passengers129
Crew10
Fatalities0
Injuries32 (2 serious)
Survivors139

Overseas National Airways (ONA) Flight 032 was a non-scheduled positioning flight operated by Overseas National Airways with a McDonnell Douglas DC-10-30CF.[1][2] On November 12, 1975, the flight crew initiated a rejected takeoff after accelerating through a large flock of gulls at John F. Kennedy International Airport, resulting in a runway excursion. Of the 139 aircraft occupants, all survived, while the aircraft was destroyed by an intense post-crash fire.[3] The National Transportation Safety Board concluded that the probable cause of the accident was bird ingestion into the right-hand engine, causing an uncontained engine failure that ruptured several landing gear tires and disabled the engine's hydraulic system, in turn partially disabling the spoilers and the landing gear brakes. Contributing to the accident was the resultant failure of the affected engine's thrust reverser and the wet runway.[1] The accident aircraft is claimed to be the largest commercial airliner ever destroyed due to a bird strike.[4]

Aircraft and crew[]

Aircraft[]

The aircraft was a 2-year-old McDonnell Douglas DC-10-30CF registered as N1032F and named "HolidayLiner Freedom" by Overseas National Airways (ONA), its only operator. It was powered by three General Electric CF6-50A high-bypass turbofan engines.[1][5]

Crew[]

The crew consisted of Captain Harry R. Davis, aged 55, employed by ONA since 1951, who had qualified to fly the DC-10 in 1973 and accumulated 25,000 flight hours in his career with 2,000 hours on the DC-10; First Officer Raymond A. Carrier, aged 52, employed by ONA since 1968, with 14,500 flight hours of which 450 hours were on the DC-10; and Flight Engineer Jack A. Holland, aged 44, employed by ONA since May 19, 1959, with 12,000 flight hours of which 2,000 flight hours were on the DC-10. In addition to the flight crew, a non-flying ONA observer occupied the jump seat in the cockpit.[1][6]

Flight[]

Onboard the flight were 129 passengers and ten crew members, all of whom were ONA employees (including maintenance crew, flight attendants, ground personnel, etc.) bound for Mecca to operate air charter flights.[1][6][7] Prior to departure, the aircraft had been loaded to 555,000 pounds (252,000 kg)—1,000 pounds (450 kg) less than its maximum takeoff weight—and was carrying an estimated 235,000 pounds (107,000 kg) of jet fuel at the time of the accident. Meteorological information indicated that visibility was 15 miles (24 km), wind was blowing at heading 160° at 8 knots (15 km/h), with an overcast ceiling of 10,000 feet (3,000 m). The captain requested Runway 13R, one of the newest runways at John F. Kennedy International Airport, due to the aircraft's heavy weight. Flight 032 entered Runway 13R at started its takeoff roll.[2][3]

Accident[]

As the DC-10 was accelerating on the ground at around 100 knots (190 km/h), a large flock of gulls rose from the runway and clustered directly in front of the aircraft. As the aircraft passed through the flock, the flight crew heard three loud explosions or bangs. The captain immediately initiated a rejected takeoff, brought the thrust levers to the idle position, and deployed the thrust reversers. The master caution lights illuminated and the flight engineer exclaimed that they had "lost" the #3 engine (the engine on the right wing) as it went into reverse thrust. The flight engineer then noticed that pressure in the #2 hydraulic system, which is powered by the #3 engine, had dropped to zero. The master fire warning lights and the fire warning light for the #3 engine illuminated, and the first officer and flight engineer attempted to shut the engine down, but found that the fuel shutoff lever would not move. The flight engineer then actuated the fire extinguishers for the engine but did not see the light that indicated the extinguishers had discharged. Around this time, the pilots realized that the aircraft was not decelerating normally but believed that directional control could be maintained, so they initiated a slight left-hand turn towards Taxiway Z to avoid plowing into a blast fence past the departure end of the runway. However, the aircraft left the runway pavement before reaching the taxiway, and began to shudder violently. As the aircraft came to rest on Taxiway Z, the captain pulled the fuel shutoff levers and fire handles for the other two engines, but was unable to order an emergency evacuation because the public address microphone had become displaced. The first officer opened a cockpit window and saw that the right wing was ablaze, and a cabin crew member opened the cockpit door, revealing that the cabin was filling with black smoke.[1]

N1032F, after the accident

Evacuation and wreckage[]

The flight crew initiated an evacuation through the cockpit windows using escape ropes and the cabin crew began evacuating the cabin using the evacuation slides. All 129 passengers and 10 crew members were able to evacuate, with 27 passengers suffering minor injuries and six crew members suffering minor or serious injuries, all sustained during the emergency evacuation. Although airport firefighters arrived almost immediately and began fighting the fire, HolidayLiner Freedom came to rest near an underground storm drain which began collecting draining fuel, rendering it extremely difficult for firefighters to extinguish the blaze; however, most of the fire remained confined to the crash area. However, pieces of the #3 engine struck a Pan Am tire shop near Runway 13R, damaging a tractor and causing several fuel drums to burn.[1][3]

The aircraft's left and centerline landing gear separated from the airframe while the right main landing gear had collapsed. Wreckage was scattered over an area of 8,460 feet (2,580 m) long and 1,086 feet (331 m) wide. Pieces of the #3 engine were scattered across the runway while the other two engines remained attached to the airframe.[1][3]

Investigation[]

National Transportation Safety Board[]

After an in-depth investigation for 1 year and 1 month, the National Transportation Safety Board released its final report on December 16, 1976.[1][2]The Cockpit Voice Recorder (CVR) was deemed unusable due to the massive fire that erupted and the Flight Data Recorder (FDR) inadvertently stopped while Flight 032 was accelerating to 168 knots. The NTSB highlighted that the crew performed "exceptionally well" and the fire did not penetrate far into the cabin or into the cockpit before everyone evacuated.[1]

Conclusions were as follows:[1]

  • The No. 3 hydraulic system was inoperative, which in turn, caused the loss of the No. 2 brake system and therefore the braking torque reduced to 0 percent
  • The No. 3 engine for thrust reverser was inoperative
  • At least three tires were disintegrated
  • The No. 3 system spoiler panels on each wing could not deploy
  • The runway surface was wet

Recommendations were as follows:[1]

  • The bird-control program at John F. Kennedy Airport did not effectively control the bird hazard at the airport
  • The Federal Aviation Administration and the General Electric Company failed to consider the effects of rotor imbalance on the abradable epoxy shroud material when the engine was tested for certification.

General Electric[]

The damage suffered by the fan blades of Engine #3

An investigation was carried out for the #3 engine at the General Electric Division Company in Ohio. A disassembly revealed that several engine fan blades were damaged and broken. The fuel pipes were also broken and so and the epoxy resin combusted, which in turn ignited the flames. However, the imminent cause of the accident was not the sea gulls per a General Electric employee.[3] General Electric made a speculation that the cause had to do with the portions of the landing gear being ingested into the right engine after the imminent collision which cut the fuel pipeline.[3]In order to prove that the General Electric CF6 engine was capable of withstanding a bird strike, the National Transportation Safety Board conducted a test on resistance of the same type of engine against birds.[1] The test provided results with no severe damage to any of the engine parts. Modifications to the test engine, such as increasing the distance between each fan blade, also provided similar results.[1][3]However, several changes could have been made to improve the effectiveness of the bird strike hazard.

Aftermath[]

Precaution against birds at JFK[]

It was reported that 11 other severe bird strike incidents occurred at John F. Kennedy between July and November 1975.[1][3]After the accident, a recommendation was given to the staff services to provide adequate bird strike protection. Following this recommendation, between 6:00 A.M. and 10 A.M. and 2:00 P.M. onwards, a crew of seven staff members patrol birds with sound detectors and shoot birds if with an imminent collision with an aircraft. The FAA mentioned that JFK bird hazard measures were taken on a "piecemeal" basis and insufficient for FAA standards. The FAA mandated to JFK:

  • To perform a daily runway inspection, especially near bird strike prone areas
  • To participate or create an effective bird hazard handling program
  • To eliminate several sewer outlets and dumps which attract sea gulls
  • Eliminate rodents or rabbits which attract sea gulls
  • Eliminate trees in the immediate area, especially bird-loved areas[8]

Engine hazard protection[]

The Federal Aviation Administration and the National Transportation provided a recommendation to General Electric about bird strike protection to the CFM-50 and CFM-6 series engines stating that the epoxy resin must be replaced with an Aluminium Honeycomb which will reduce the contained damage the critical and fragile engine compressor.[9][10]

Seat belt recommendation[]

On June 15, 1978, a recommendation was also sent to American Safety Inc. that the restraints on the ONA DC-10's involving this and another non-fatal accident in Turkey in 1976 were not sufficient.[11] Between 7 - 10 inches of the 19 inches of maximum pull, the seatbelt would provide the lock mechanism required as one flight attendant in this accident was thrown off from her jumpseat and in the accident in Turkey, three flight attendants were thrown off from their jumpseats.[12]

See also[]

References[]

  1. ^ a b c d e f g h i j k l m n o "NATIONAL TRANSPORTATION SAFETY BOARD - OVERSEAS NATIONAL AIRWAYS DOUGLAS DC-10-30CF - AAR76/19" (PDF). Retrieved November 30, 2021.{{cite web}}: CS1 maint: url-status (link)
  2. ^ a b c Ranter, Harro. "ASN Aircraft accident McDonnell Douglas DC-10-30CF N1032F New York-John F. Kennedy International Airport, NY (JFK)". aviation-safety.net. Retrieved 2021-12-01.
  3. ^ a b c d e f g h "Lessons Learned". lessonslearned.faa.gov. Retrieved 2021-11-30.
  4. ^ Brotak, Ed (2018-03-23). "When Birds Strike". HistoryNet. Retrieved 2021-12-07.
  5. ^ Noack, Thomas. "N1032F Overseas National Airways (ONA) McDonnell Douglas DC-10-30". www.planespotters.net. Retrieved 2021-11-30.{{cite web}}: CS1 maint: url-status (link)
  6. ^ a b "Overseas National Airways Crew Friendship Site". www.onacrew.com. Retrieved 2021-11-30.
  7. ^ Lisbowilz, Richard Witkin The New York Times/Meyer (1975-11-13). "139 ESCAPE DC‐10 AFIRE AT KENNEDY". The New York Times. ISSN 0362-4331. Retrieved 2021-11-30.
  8. ^ Aviation, United States Congress House Committee on Public Works and Transportation Subcommittee on (1979). Aviation Safety, DC-10 Crash of May 25, 1979: Joint Hearings Before the Subcommittee on Aviation and the Subcommittee on Oversight and Review of the Committee on Public Works and Transportation, House of Representatives, Ninety-sixth Congress, First Session, June 19 and 20, 1979. U.S. Government Printing Office. pp. 249–251.
  9. ^ "Airworthiness Directive Recommendation for GENERAL ELECTRIC Models CF6-50A, CF6-50C, CF6-50D, CF6-50E, CF6-50E1 and CF6-50H Engines" (PDF). Federal Aviation Administration. Retrieved December 6, 2021.{{cite web}}: CS1 maint: url-status (link)
  10. ^ "Airworthiness Directive Recommendation for GENERAL ELECTRIC Models CF6-6D and CF6-6D1 Engines" (PDF). Federal Aviation Administration. Retrieved December 6, 2021.{{cite web}}: CS1 maint: url-status (link)
  11. ^ Ranter, Harro. "ASN Aircraft accident McDonnell Douglas DC-10-30CF N1031F Istanbul-Yesilköy Airport (IST)". aviation-safety.net. Retrieved 2021-12-07.
  12. ^ "Aviation Safety, DC-10 Crash of May 25, 1979: Joint Hearings Before the ... - United States. Congress. House. Committee on Public Works and Transportation. Subcommittee on Aviation - Google Books". Google Books. 1979. pp. 247–248. Retrieved December 6, 2021.{{cite web}}: CS1 maint: url-status (link)

External links[]

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